Fukunaga & Associates, Inc.

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Ford Island Waterline Replacement

FI_Photo 1Summary and Description

A new 24-inch (ID) high-density polyethylene water main was installed beneath Pearl Harbor utilizing an innovative directional drilling and underwater splicing procedure that has greatly improved the performance and reliability of the Navy’s water distribution system. The applied method avoided environmental disturbances associated with conventional underwater pipe laying operations.

Background

The primary water transmission main that serves Ford Island and the Pearl Harbor Naval Complex is over 75 years old. Failure of this primary line exposes the existing and proposed developments on Ford Island and potentially the Pearl Harbor Naval Shipyard to extended water supply outages and possible interruption or impairment of essential activities within the Naval Complex. A new replacement line was programmed and installed as part of this project to improve the reliability of the water system serving Pearl Harbor. Fukunaga & Associates, Inc. was selected by the Naval Facilities Engineering Command Pacific (NAVFAC Pacific) to provide engineering services to design the new replacement waterline.

Consultant’s Role in the Project
Fukunaga & Associates, Inc. (FAINC) served as the prime engineering consultant for the project, as well as the civil design engineer. As the prime consultant, FAINC handled all project management responsibility and coordination with the client (NAVFAC Pacific)FI_2 and the water system owner (NAVFAC, Hawaii). Subconsultants for the project included: URS Corporation of Honolulu— geotechnical engineers and HDD consultant, MK Engineers, Ltd.—Electrical Engineers, and SLSH, Inc.— Structural Engineers.

The design process for this project included a Functional Analysis Concept Development (FACD) study that brought together all stakeholders associated with the project. Participants included the project owner – NAVFAC, Hawaii; the client – NAVFAC Pacific; and the design team. The FACD effort defined the project scope, and emphasized the need for a commitment from all participants to work together towards a successful project, meeting the owner/client objectives and keeping within the available funding and project schedule. The commitment was formalized in a Partnering Agreement that documented the project scope and basis of design. The Agreement was signed by representatives of the Owner, Client and Fukunaga & Associates, Inc.—the prime consultant for the design team. This spirit of partnership and commitment carried throughout the project development and implementation, resulting in a final product that met the owner’s objectives and exceeded the expectations of improved system performance.

Innovative Application of New and Existing Techniques
Horizontal Directional Drilling techniques are now fairly well developed and have been applied to numerous projects throughout the world. However, in this project, an extension of conventional HDD techniques was applied to address several unique conditions facing the design team.FI_3 The first, and potentially the most difficult and costly challenge, was the under channel crossing beneath Pearl Harbor. From shoreline to shoreline, the crossing would need to cover over 5,000 linear feet. It would not be possible to make this crossing in a single pull using conventional HDD methods with thermoplastic pipe.
Alternatives considered included using HDD methods of pulling a steel casing beneath the channel and then performing a second pull to insert a plastic pipe through the casing. Then the annular space between the plastic pipe and steel casing would need to be pressure grouted to support the plastic waterline. Non- HDD alternatives included conventional underwater pipe laying by dredging a trench along the channel bottom and installing a pipe, then backfilling the trench underwater. This operation would almost certainly cause significant disturbance to the channel bottom, and raised the concern of unleashing potentially hazardous sediment into the Harbor waters. Implementation of mitigative measures and water quality monitoring would add significant costs to this alternative. Furthermore, the proposed crossing alignment was adjacent to the new Admiral Clarey Bridge that connects Ford Island to the landside.
Impacts of dredging, pipe laying and backfill operations could jeopardize the stability of the bridge foundation system. Since the channel would need to accommodate some of the largest ships in the U.S. Navy’s fleet (aircraft carriers), the pipeline would need to be at least 10 feet below the channel bottom. This meant significant underwater excavation and backfill.
The selected installation method was developed through a joint effort of FAINC and their geotechnical/HDD subconsultant, URS. A dual bore operation and underwater splice was considered as an alternative early in the conceptual design development for the project. However, there were concerns that creating a midcrossing high point underwater could potentially trap residual air bubbles and cause operational problems. Air trapped in the pipeline would reduce the carrying capacity of the transmission line and possibly cause air-binding that could prevent water flow through the pipe.
FI_4Careful inspection of a bathymetric survey of the harbor bottom identified a distinct drop-off after a shallow shelf on the northeast shore of Ford Island. By using two separate bores, with one starting from the Ford Island side (Bore No. 2), exiting at the toe of the steep drop-off, and the second starting from the Halawa shore (Bore No. 1) exiting just past the navigation channel, a continuous, sweeping profile through the underwater splice would be possible without creating a high-point under the channel. (The design profile is illustrated in Figure 2.) The underwater splice was backfilled with clean, crushed aggregate and covered with an articulated concrete matting system. This was done to protect the pipeline, and also to provide ballast to keep the pipeline permanently anchored in place. Providing the proper ballast volume and weights for the pipeline were crucial to insure stability throughout the underwater installation process, as well as for the permanent installation.

The remainder of the waterline network on Ford Island was installed utilizing both conventional HDD and open trench operations. In all, approximately 19,550 linear feet of pipeline was installed on Ford Island. The total project construction cost was $12.0 million, which was well below the estimated construction cost (ECC) program budget of $12.6 million.

Technical Value to the Engineering Profession

This project demonstrates how existing technologies can be extended beyond conventional applications to provide effective solutions. The two bore horizontal directional drilling and pipe string method used in this project exceeded conventional single point bore applications. The two bore method allowed the installation of a pipeline twice the length expected under conventional HDD operations. Of course, the use of dive operations for the underwater splice connection was required; however, this underwater work was substantially less than would be required for typical underwater pipe laying construction.

Social, Economic and Sustainable Design Considerations
Among the primary considerations for the project was the need to improve the efficiency and reliability of the Navy’s Pearl Harbor water system. This project provided much needed carrying capacity as well as backup capability for the water system to maintain water service to all base activities. As a result of the new line, and with improvements to the overall system, the pumps driving the water system have been operating more efficiently due to the reduced system back pressure. The lower system operating pressure has basically resulted in lower energy consumption and greater delivery capability. NAVFAC, Hawaii estimates of energy cost savings attributed to the system improvements are currently about $50,000 per year.

FI_5The application of trenchless construction methods used in this project also resulted in minimal impact on the environment. Of specific concern was the underwater crossing work that may have caused significant disturbance to the sediments on the Harbor bottom. It was imperative that the Harbor waters not be clouded with suspended sediment that may contain hazardous or toxic materials. The pipeline materials used in the project were selected for their corrosion resistant properties, with the intent of providing maximum service life. Furthermore, serviceable items such as valves and expansion couplings are installed in concrete vaults that allow service and replacement without the need to excavate large areas, reducing future impacts on the surrounding areas.

Complexity
Various design elements were considered as part of the modified HDD method, including vertical alignment for minimum pipe bend radius, pulling loads on the High-Density Polyethylene pipe string, hydraulic design to avoid a mid-length high point, and permanent harbor bottom ballast to maintain the long term stability of the installed pipeline.
Containment of HDD drill fluids at the mid-harbor exit locations required adopting special provisions to prevent contamination of the harbor waters.

Borehole stability, and heave and hydro-fracture potential were assessed for various drilling fluid scenarios. Risk of consequential damage to the adjacent pile supported Admiral Clarey Bridge from potential hydro-fracture or borehole collapse was also evaluated using finite element analysis of combined pipe and bridge soil-structure interaction, confirming HDD to be the preferred solution as compared to underwater cut and cover (trenching) methods. Construction observations were also vital for project success, including offshore Tru-Tracker drill head navigation to insure proper borehole alignment, avoiding encroachment into the bridge foundation support zone and eliminating high points in the smooth sweeping pipeline profile. Constant monitoring of pull loads was also required to avoid overstressing the pipe string, which could potentially permanently impair the pressure rating and longevity of the waterline. Surface barge staging operations, with an assist rig to provide support of the pipeline during the over water staging and pipe string insertion operations, were required. Also, dive operations for the final underwater splice connection were also required to complete the installation of the submarine line.

Meeting and Exceeding the Client’s Expectations
FAINC and the design team were fully engaged in support of the project from inception, through development, and final completion, partnering with both the client (NAVFAC Pacific) and the ownerFI_6 (NAVFAC, Hawaii), as formalized in the FACD effort. As with most projects the construction cost was a major concern. It was a significant challenge to meet project objectives within the available budget. For this project, the original programming documents had set the ECC at $12.6 million. The final design construction cost estimate was $12.1 million, and the actual final construction cost was $12.0 million. Much of the cost savings can be attributed to the innovative design of the under channel pipeline crossing.
The greatest long-term benefits to the Navy will be from more energy efficient operations and enhanced system reliability. The new water system installed on Ford Island will support proposed developments that will transform the island into a vibrant commercial, visitor and operations center within Pearl Harbor.

The design team completed the project on time and within the design budget, earning a Certificate of Appreciation from the Navy for “outstanding design and engineering services, responsiveness and highest level of professionalism.” The project was put out to bid on schedule in 2002, with construction commencing, also as scheduled, in 2003. The project was substantially completed in 2005. The waterline was operational and ready to support several key Ford Island facilities including the National Oceanic & Atmospheric Administration Pacific Regional Center and Ship Operations Facility (under construction), the Pacific Warfighting Center (in design), and the Pacific Aviation Museum (under construction).

  • Current Projects
  • Award Winning Projects
    • Ala Moana Wastewater Pump Station Force Mains #3 & #4
    • Pearl Harbor Channel Underwater Waterline Crossing
    • Kaneohe Bay Drive Trunk Sewer Reconstruction
    • Ford Island Waterline Replacement
    • FY01 MCON Project P-491
    • Long Range Sewer Rehabilitation
    • Kihei Effluent Reuse System
  • Past Projects
    • General Civil Projects
    • Wastewater Projects
    • Water Projects
  • Project Gallery